On 17. 10. 19 14:59, Thierry Reding wrote:
On Thu, Oct 17, 2019 at 02:09:17PM +0200, Uwe Kleine-König wrote:
On Thu, Oct 17, 2019 at 01:11:31PM +0200, Thierry Reding wrote:
On Thu, Oct 17, 2019 at 12:11:16PM +0200, Uwe Kleine-König wrote:
On Thu, Oct 17, 2019 at 11:48:08AM +0200, Michal Vokáč wrote:
On 17. 10. 19 10:10, Uwe Kleine-König wrote:
A previous change in the pwm core (namely 01ccf903edd6 ("pwm: Let
pwm_get_state() return the last implemented state")) changed the
semantic of pwm_get_state() and disclosed an (as it seems) common
problem in lowlevel PWM drivers. By not relying on the period and duty
cycle being retrievable from a disabled PWM this type of problem is
worked around.

Apart from this issue only calling the pwm_get_state/pwm_apply_state
combo once is also more effective.

Signed-off-by: Uwe Kleine-König <u.kleine-koe...@pengutronix.de>
---
Hello,

There are now two reports about 01ccf903edd6 breaking a backlight. As
far as I understand the problem this is a combination of the backend pwm
driver yielding surprising results and the pwm-bl driver doing things
more complicated than necessary.

So I guess this patch works around these problems. Still it would be
interesting to find out the details in the imx driver that triggers the
problem. So Adam, can you please instrument the pwm-imx27 driver to
print *state at the beginning of pwm_imx27_apply() and the end of
pwm_imx27_get_state() and provide the results?

Note I only compile tested this change.

Hi Uwe,
I was just about to respond to the "pwm_bl on i.MX6Q broken on 5.4-RC1+"
thread that I have a similar problem when you submitted this patch.

So here are my few cents:

My setup is as follows:
  - imx6dl-yapp4-draco with i.MX6Solo
  - backlight is controlled with inverted PWM signal
  - max brightness level = 32, default brightness level set to 32 in DT.

1. Almost correct backlight behavior before 01ccf903edd6 ("pwm: Let
    pwm_get_state() return the last implemented state):

  - System boots to userspace and backlight is enabled all the time from
    power up.

    $ dmesg | grep state
    [    1.763381] get state end: -1811360608, enabled: 0

What is -1811360608? When I wrote "print *state" above, I thought about
something like:

        pr_info("%s: period: %u, duty: %u, polarity: %d, enabled: %d",
                __func__, state->period, state->duty_cycle, state->polarity, 
state->enabled);

A quick look into drivers/pwm/pwm-imx27.c shows that this is another
driver that yields duty_cycle = 0 when the hardware is off.

It seems to me like the best recourse to fix this for now would be to
patch up the drivers that return 0 when the hardware is off by caching
the currently configured duty cycle.

How about the patch below?

Thierry

--- >8 ---
 From 15a52a7f1b910804fabd74a5882befd3f9d6bb37 Mon Sep 17 00:00:00 2001
From: Thierry Reding <thierry.red...@gmail.com>
Date: Thu, 17 Oct 2019 12:56:00 +0200
Subject: [PATCH] pwm: imx27: Cache duty cycle register value

The hardware register containing the duty cycle value cannot be accessed
when the PWM is disabled. This causes the ->get_state() callback to read
back a duty cycle value of 0, which can confuse consumer drivers.

Signed-off-by: Thierry Reding <thierry.red...@gmail.com>
---
  drivers/pwm/pwm-imx27.c | 31 ++++++++++++++++++++++++-------
  1 file changed, 24 insertions(+), 7 deletions(-)

diff --git a/drivers/pwm/pwm-imx27.c b/drivers/pwm/pwm-imx27.c
index ae11d8577f18..4113d5cd4c62 100644
--- a/drivers/pwm/pwm-imx27.c
+++ b/drivers/pwm/pwm-imx27.c
@@ -85,6 +85,13 @@ struct pwm_imx27_chip {
        struct clk      *clk_per;
        void __iomem    *mmio_base;
        struct pwm_chip chip;
+
+       /*
+        * The driver cannot read the current duty cycle from the hardware if
+        * the hardware is disabled. Cache the last programmed duty cycle
+        * value to return in that case.
+        */
+       unsigned int duty_cycle;
  };
#define to_pwm_imx27_chip(chip) container_of(chip, struct pwm_imx27_chip, chip)
@@ -155,14 +162,17 @@ static void pwm_imx27_get_state(struct pwm_chip *chip,
        tmp = NSEC_PER_SEC * (u64)(period + 2);
        state->period = DIV_ROUND_CLOSEST_ULL(tmp, pwm_clk);
- /* PWMSAR can be read only if PWM is enabled */
-       if (state->enabled) {
+       /*
+        * PWMSAR can be read only if PWM is enabled. If the PWM is disabled,
+        * use the cached value.
+        */
+       if (state->enabled)
                val = readl(imx->mmio_base + MX3_PWMSAR);
-               tmp = NSEC_PER_SEC * (u64)(val);
-               state->duty_cycle = DIV_ROUND_CLOSEST_ULL(tmp, pwm_clk);
-       } else {
-               state->duty_cycle = 0;
-       }
+       else
+               val = imx->duty_cycle;
+
+       tmp = NSEC_PER_SEC * (u64)(val);
+       state->duty_cycle = DIV_ROUND_CLOSEST_ULL(tmp, pwm_clk);
if (!state->enabled)
                pwm_imx27_clk_disable_unprepare(chip);
@@ -261,6 +271,13 @@ static int pwm_imx27_apply(struct pwm_chip *chip, struct 
pwm_device *pwm,
                writel(duty_cycles, imx->mmio_base + MX3_PWMSAR);
                writel(period_cycles, imx->mmio_base + MX3_PWMPR);
+ /*
+                * Store the duty cycle for future reference in cases where
+                * the MX3_PWMSAR register can't be read (i.e. when the PWM
+                * is disabled).
+                */
+               imx->duty_cycle = duty_cycles;
+

I wonder if it would be more sensible to do this in the pwm core
instead. Currently there are two drivers known with this problem. I
wouldn't be surprised if there were more.

I've inspected all the drivers and didn't spot any beyond cros-ec and
i.MX that have this problem. There's also no good way to do this in the
core, because the core doesn't know whether or not the driver is capable
of returning the correct duty cycle on hardare readout. So the core
would have to rely on state->duty_cycle that is passed in, but then the
offending commit becomes useless because the whole point was to return
the state as written to hardware (rather than the software state which
was being returned before that patch).

If we want to move clients to not rely on .period and .duty_cycle for a
disabled PWM (do we?) a single change in the core is also beneficial
compared to fixing several lowlevel drivers.

These are really two orthogonal problems. We don't currently consider
enabled = 0 to be equivalent to duty_cycle = 0 at an API level. I'm not
prepared to do that at this point in the release cycle either.

What this here has shown is that we have at least two drivers that don't
behave the way they are supposed to according to the API and they break
consumers. If they break for pwm-backlight, it's possible that they will
break for other consumers as well. So the right thing to do is fix the
two drivers that are broken.

After -rc1 we no longer experiment. Instead we clean up the messes we've
made. We can revisit the other points once mainline is fixed.

Hi Thierry,
I just tried your patch with v5.4-rc3 with this result:

root@hydraco:~# dmesg | grep pwm_
[    1.772089] pwm_imx27_get_state: period: 992970, duty: 0, polarity: 0, 
enabled: 0
[    4.938759] pwm_imx27_apply: period: 500000, duty: 0, polarity: 1, enabled: 0
[    4.947431] pwm_imx27_get_state: period: 992970, duty: 0, polarity: 0, 
enabled: 0
[    4.956484] pwm_imx27_apply: period: 992970, duty: 992970, polarity: 0, 
enabled: 0
[    4.965473] pwm_imx27_get_state: period: 992970, duty: 0, polarity: 0, 
enabled: 0
[    4.974410] pwm_imx27_apply: period: 992970, duty: 0, polarity: 0, enabled: 1
[    4.988617] pwm_imx27_get_state: period: 992970, duty: 0, polarity: 0, 
enabled: 1

Backlight is on with full brightness at this stage.

root@hydraco:/sys/class/backlight/backlight# cat brightness
32

root@hydraco:/sys/class/backlight/backlight# echo 32 > brightness
[  153.386391] pwm_imx27_apply: period: 992970, duty: 992970, polarity: 0, 
enabled: 1
[  153.398311] pwm_imx27_get_state: period: 992970, duty: 992970, polarity: 0, 
enabled: 1

Backlight goes down.

root@hydraco:/sys/class/backlight/backlight# echo 1 > brightness
[  168.506261] pwm_imx27_apply: period: 992970, duty: 15576, polarity: 0, 
enabled: 1
[  168.518064] pwm_imx27_get_state: period: 992970, duty: 15576, polarity: 0, 
enabled: 1

Backlight goes up to almost full brightness.

root@hydraco:/sys/class/backlight/backlight# echo 0 > brightness
[  177.496265] pwm_imx27_apply: period: 992970, duty: 0, polarity: 0, enabled: 0
[  177.507602] pwm_imx27_get_state: period: 496485, duty: 7788, polarity: 0, 
enabled: 0

Backlight goes up to full brightness.

So your patch does not solve my issue.

The main problem I see is incorrect polarity setting. In my DT
the pwm-backlight consumer requests PWM_POLARITY_INVERTED and
period 500000ns. Though after reset the PWM HW registers are
configured to normal polarity. This initial setting is read out
and used by the consumer instead of the DT configuration.

Michal
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