> Ignore the air compressor behind the curtain!  (Sorry we just watched
the
> wizard of oz recently).

He, he..  before deciding on the Jun-Air compressor wanted to get some
test time and size the volume and flow rates.  OTOH one could just stick
the el-cheapo unit in a separate room and run a long supply line to say an
intermediate storage tank.

Looks great, and sounds like you are getting a
> lot
> of bang for the buck with this approach!
>

Also *discovering* some interesting design issues that need working; e.g.

1) a victim of my own success.  the bellcrank, connections, and mount
points all use bearings; friction is sooo low that have to account for the
weight of the column.  move it a few degress off vertical either way and
it flops to the end stop.

2) the high res pot gearing and connection to the column results in a
non-linear reporting of the position; i.e. from full forward to vertical
is 10 degrees, the pot reports 250 to 1900, from vertical to full aft is
25 degrees, the pot reports from 1900 to 3800.  at least the roll channel
is linear;  1000 (full left) to 2000 (center) to 3000 (full right)

3) have to account for the difference in surface area of the linear
actuator piston due to the actuator rod, at least that is a FIXED
value/ratio ;-)  the rotary rack and pinion actuator for the roll channel
has equal surface area on both sides of the piston

4) there is a little hystersis in the system, when disturbed the column
returns to around 1%, for a setpoint of 2000 that results in a value of
2020 to 1980 which is really not all that bad but it grows some the
further off the vertical one moves.  Test data shows the *error* is
consistent. had to design a virtual bobweight that countered the
off-center moment created by the column, so that needs some tuning. 
Probably also do some more work on the PD control algorithm. Response
times are quite acceptable, but still have to get it wired into
flightgear, work on a control loading algorithm in JSBSim and then some
flight testing.  But I'm very encouraged by the results so far

5) the really good news is the motion and action is very smooth and steady,
force gradients in either direction from the setpoint increase
monotonically and are precise, and no apparent glitch, jerk, or bump when
moving through the neutral stick position( setpoint); change in force is
VERY smooth.  Currently, working at a very low psi level, in the order of
the 5-12 psi range and the forces generated are quite substantial while
requiring minimum CFM.  Will probably move to a higher level to factor in
such items as Q (dynamic pressure) and G-loading

Hooking up an autopilot is going to be a real blast!

again, really liked the low cost aspects. the electro-regulators cost
$1200 and the actuators $330, the filtering system including the mist
seperator for oil-lubed compressor around $100,  miscellaneous tubing,
connectors, and exhuast silencers another $100,  the USB controller card
and chips about $150.  So for around $2K one can build a substantial
control force loading system for both the pitch and roll channels.

Still need to post those pics. Just haven't had the time to figure out how
to handle inputting stuff to the wiki page and not sure it is a good fit.
Thought about the company site, but ATM that site is down as we're moving
it to a new ISP.

Also taking the opportunity to rebuild portions of the sim while it is
disassembled,  adding panels to the center pedestal for nav/radio/iff
controls and major rework of the auto-throttles. Redoing the electronics
based in part on the design changes we made for the AeroNvironment GO
program. Lot more capacity for additional switches, rotaries, and
lights/LEDS, as well as all panels will be backlighted.

Jack





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