From: Kazuya Mizuguchi <[email protected]>

Set PHY rxc-skew-ps to 1500 and all other values to their default values.

This is intended to to address failures in the case of 1Gbps communication
using the by salvator-x board with the KSZ9031RNX phy. This has been
reported to occur with both the r8a7795 (H3) and r8a7796 (M3-W) SoCs.

Signed-off-by: Kazuya Mizuguchi <[email protected]>
Signed-off-by: Takeshi Kihara <[email protected]>
Signed-off-by: Simon Horman <[email protected]>

---
v1 [Simon Horman]
* Do not set values to defaults, omit them and let the driver set the defaults
* Rewrote changelog

  N.B. The communications failures have been reported by the BSP team,
       however I did not observe them during testing with a
       salvator-x/M3-W-ES1.0

       My test-case was to bring up the system using NFS root and
       run: netperf -H <HOST>

v0 [Kazuya Mizuguchi]
---
 arch/arm64/boot/dts/renesas/r8a7796-salvator-x.dts | 13 +------------
 1 file changed, 1 insertion(+), 12 deletions(-)

diff --git a/arch/arm64/boot/dts/renesas/r8a7796-salvator-x.dts 
b/arch/arm64/boot/dts/renesas/r8a7796-salvator-x.dts
index 61f4662db497..93ed23ab71bb 100644
--- a/arch/arm64/boot/dts/renesas/r8a7796-salvator-x.dts
+++ b/arch/arm64/boot/dts/renesas/r8a7796-salvator-x.dts
@@ -172,18 +172,7 @@
        status = "okay";
 
        phy0: ethernet-phy@0 {
-               rxc-skew-ps = <900>;
-               rxdv-skew-ps = <0>;
-               rxd0-skew-ps = <0>;
-               rxd1-skew-ps = <0>;
-               rxd2-skew-ps = <0>;
-               rxd3-skew-ps = <0>;
-               txc-skew-ps = <900>;
-               txen-skew-ps = <0>;
-               txd0-skew-ps = <0>;
-               txd1-skew-ps = <0>;
-               txd2-skew-ps = <0>;
-               txd3-skew-ps = <0>;
+               rxc-skew-ps = <1500>;
                reg = <0>;
                interrupt-parent = <&gpio2>;
                interrupts = <11 IRQ_TYPE_LEVEL_LOW>;
-- 
2.7.0.rc3.207.g0ac5344

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