KR> water injection installed

2016-07-30 Thread Mark Langford
NetHeads,

After years of threatening to do it, I finally got around to installing 
water injection on my plane, and test flew it today.

I ran water injection on my 2110cc Karmann Ghia back in the late 70's 
when I lived in the desert, to tame the detonation caused by the 9.9:1 
compression ratio (lots of long stories in that sentence).   It was only 
activated above certain throttle settings using an adjustable vacuum 
switch, squirting water down the throats of twin Weber 40IDF carbs, and 
worked quite well.  What I didn't realize is that water injection also 
"steam cleans" piston tops and combustion chambers, because when I 
pulled the heads to lower the compression, the chambers and piston tops 
looked like new!

I don't have detonation problems with the latest incarnation of my 
2180cc airplane engine, especially since I dropped the compression ratio 
to 8.1:1 so I could run 93 octane auto fuel on the hottest summer days, 
but I do like the idea of keeping the chambers and pistons squeaky clean 
and deposit free.  So I found a "windshield washer kit" on ebay for $12 
that uses a pliable plastic bag for the reservoir, allowing me to easily 
fasten it to my engine mount in an area that is otherwise quite tight on 
space.

I can report today that running the injection at near wide open throttle 
is barely perceptible, indicated only by a 20-30 rpm drop in RPM, and it 
makes the engine run slightly leaner, according to the mixture meter.  I 
installed the push-button switch that came with the kit, but only used a 
pint or so of water in two minutes of operation, so I'll probably 
install a toggle switch so I can run it for 10 minutes to empty the bag 
and do some serious cleaning.

I welded primer port fittings into the intake manifold for each cylinder 
(total of four), with a standard .020" diameter primer nozzle installed 
in each cylinder's inlet manifold runner for the primer system.  Since 
the engine starts without priming in the summer, I simply disconnected 
the fuel line and slipped the plastic tubing into the tee that goes to 
each side.  Works like a charm.  I was concerned about the primer 
nozzles sucking water out of the bag at high vacuum (idle), so I also 
bought a $10 "pneumatic" 12V solenoid (a Keurig coffee maker replacement 
part) from ebay so water only flows when I want it to.

Although this likely falls under the heading of "stuff you don't need", 
I like the idea of having clean combustion chambers and piston tops, and 
a quick way to quell detonation should it ever happen with this low 
compression ratio.  Obviously, this won't work in freezing temperatures, 
but it's not needed for detonation in the winter anyway.  See enclosed 
photo for my rather shoddy (but temporary) installation, but it does 
work fine this way.  As you can see, real estate is limited, so a normal 
hard plastic reservoir wouldn't fit.  All electrical connections are 
insulated and there's a fuse and a breaker in the line also.

See http://www.n56ml.com/ghia2.jpg for a picture of the Ghia (still got 
it), and see the water injection "installation" photo below this message 
as an attachment.

-- 
Mark Langford
ML at N56ML.com
http://www.n56ml.com

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KR> (no subject)

2016-07-30 Thread Earl Klinker
I am very happy to see that all who went to OSH have returned home safe 
and all had a good time.

Regards

Earl Klinker

Palm Harbor, FL




KR> 0-200/happy/Oshkosh

2016-07-30 Thread Rob Schmitt
Just returned home myself from OSH. Approx 9 hours flight time. 5 up and 4 back 
to Kansas City. I did visit the Tailwind fly-in in Watertown WI on the way up.

Most interesting item from this week was the iLevel system coupled to an IPad. 
One Tailwind pilot was using this with the IPad for all his flight instruments 
- no back up. It has a pitot and static ports as part of the set up. 

My KR flew great as usual. Tons of fun was had. 

Much thanks to Larry Howell and his wife Gwen for hosting as well!

Rob Schmitt
N1852Z


> On Jul 30, 2016, at 11:53 AM, Larry Flesner via KRnet  list.krnet.org> wrote:
> 
> 
> 
> Mark Langford and I flew loose formation on the 426 s.m. trip from my home 
> base to Oshkosh last Saturday morning.  We departed "special VFR" to overcome 
> lingering fog.  Mark probably has speeds, etc.., I don't.
> 
> My hour meter (clock time)  recorded 7.1 hours total round trip with 2 fuel 
> stops (one up, one back) so there was 5 taxi in and taxi out in that time.  I 
> left with 5 1/2 quarts of oil and 1/2 quart of Marvel Mystery oil in the 
> tank.  I checked the oil this morning and still have 5 1/4 quarts in the tank 
> and it is still amber looking after 22 hours since oil change.  Not bad for 
> an engine with 2400 + hours since factory overhaul.  I'm happy with that.  
> Now I'm trying to justify overhauling it this winter.
> 
> Fun time at Oshkosh.  Thanks to Larry and Gwen Howell for putting up with 
> Mark and I at their camp site.  One of a kind hosts for sure.
> 
> See you all at the Gathering.
> 
> Larry Flesner
> flesner/at/frontier.com
> 
> 
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KR> 0-200/happy/Oshkosh

2016-07-30 Thread Larry Flesner


Mark Langford and I flew loose formation on the 426 s.m. trip from my 
home base to Oshkosh last Saturday morning.  We departed "special 
VFR" to overcome lingering fog.  Mark probably has speeds, etc.., I don't.

My hour meter (clock time)  recorded 7.1 hours total round trip with 
2 fuel stops (one up, one back) so there was 5 taxi in and taxi out 
in that time.  I left with 5 1/2 quarts of oil and 1/2 quart of 
Marvel Mystery oil in the tank.  I checked the oil this morning and 
still have 5 1/4 quarts in the tank and it is still amber looking 
after 22 hours since oil change.  Not bad for an engine with 2400 + 
hours since factory overhaul.  I'm happy with that.  Now I'm trying 
to justify overhauling it this winter.

Fun time at Oshkosh.  Thanks to Larry and Gwen Howell for putting up 
with Mark and I at their camp site.  One of a kind hosts for sure.

See you all at the Gathering.

Larry Flesner
flesner/at/frontier.com