2.6.33-longterm review patch.  If anyone has any objections, please let us know.

------------------

From: Igor Grinberg <grinb...@compulab.co.il>

commit 6c7b3ea52e345ab614edb91d3f0e9f3bb3713871 upstream.

While in sleep mode the CS# and other V3020 RTC GPIOs must be driven
high, otherwise V3020 RTC fails to keep the right time in sleep mode.

Signed-off-by: Igor Grinberg <grinb...@compulab.co.il>
Signed-off-by: Eric Miao <eric.y.m...@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gre...@suse.de>

---
 arch/arm/mach-pxa/cm-x300.c |    8 ++++----
 1 file changed, 4 insertions(+), 4 deletions(-)

--- a/arch/arm/mach-pxa/cm-x300.c
+++ b/arch/arm/mach-pxa/cm-x300.c
@@ -154,10 +154,10 @@ static mfp_cfg_t cm_x3xx_mfp_cfg[] __ini
        GPIO99_GPIO,                    /* Ethernet IRQ */
 
        /* RTC GPIOs */
-       GPIO95_GPIO,                    /* RTC CS */
-       GPIO96_GPIO,                    /* RTC WR */
-       GPIO97_GPIO,                    /* RTC RD */
-       GPIO98_GPIO,                    /* RTC IO */
+       GPIO95_GPIO | MFP_LPM_DRIVE_HIGH,       /* RTC CS */
+       GPIO96_GPIO | MFP_LPM_DRIVE_HIGH,       /* RTC WR */
+       GPIO97_GPIO | MFP_LPM_DRIVE_HIGH,       /* RTC RD */
+       GPIO98_GPIO,                            /* RTC IO */
 
        /* Standard I2C */
        GPIO21_I2C_SCL,


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