On Tue, Mar 26, 2024 at 1:11 PM Christian Gmeiner <christian.gmei...@gmail.com> wrote:
> It got better but the model is (still) wrong: > > U-Boot 2024.04-rc5-dirty (Mar 26 2024 - 17:03:41 +0100) > > CPU: Freescale i.MX6Q rev1.3 996 MHz (running at 792 MHz) > CPU: Extended Commercial temperature grade (-20C to 105C) at 20C > Reset cause: POR > Model: SolidRun HummingBoard2 Dual/Quad (1.5som+emmc) > Board: MX6 HummingBoard2 > DRAM: 2 GiB > Core: 82 devices, 17 uclasses, devicetree: fit > MMC: FSL_SDHC: 1, FSL_SDHC: 2 > Loading Environment from MMC... *** Warning - bad CRC, using default > environment It seems to me that there is a mix of DM GPIO and non-DM GPIO. Does the change below help? --- a/board/solidrun/mx6cuboxi/mx6cuboxi.c +++ b/board/solidrun/mx6cuboxi/mx6cuboxi.c @@ -336,20 +336,16 @@ static enum board_type board_type(void) * HB 1 1 x */ - gpio_direction_input(IMX_GPIO_NR(2, 8)); - val3 = gpio_get_value(IMX_GPIO_NR(2, 8)); + val3 = !!dm_gpio_get_value(&(board_detect_desc[0])); if (val3 == 0) return HUMMINGBOARD2; - gpio_direction_input(IMX_GPIO_NR(3, 4)); - val2 = gpio_get_value(IMX_GPIO_NR(3, 4)); + val2 = !!dm_gpio_get_value(&(board_detect_desc[1])); if (val2 == 0) return HUMMINGBOARD; - - gpio_direction_input(IMX_GPIO_NR(4, 9)); - val1 = gpio_get_value(IMX_GPIO_NR(4, 9)); + val1 = !!dm_gpio_get_value(&(board_detect_desc[2])); if (val1 == 0) { return CUBOXI;