Hi,

just send you my image via private mail.

The memory layout seems to be correct as I see it, interesting...

Cheers,
Hauke


On 04.05.2015 11:26, anand srivastava wrote:
Hi Hauke,

Those addresses seem to be proper. Checked in include/stm32f051x8.h

Is it possible to send me the image that is being built at your end.

I will try to run that one here. That will tell me whether the problem is with the compiler or the OpenOCD.

That file zipped should be about 100kb. You can send it to me directly [email protected] <mailto:[email protected]>

thanks and regards,
-anand


On Mon, May 4, 2015 at 2:27 PM, anand srivastava <[email protected] <mailto:[email protected]>> wrote:

    Hi,

    I have tried with the older GCC, still getting the same result.

    Is it possible that the problem is with the memory layout that is
    being produced by the compiler.

    (gdb) p &_etext
    $2 = (uint32_t *) 0x8003790
    (gdb) p &_erelocate
    $3 = (uint32_t *) 0x20000070 <uart_rx_mutex>
    (gdb) p &_srelocate
    $4 = (uint32_t *) 0x20000000 <heap_top>
    (gdb) p &_szero
    $5 = (uint32_t *) 0x20000070 <uart_rx_mutex>
    (gdb) p &_ezero
    $6 = (uint32_t *) 0x20000718
    (gdb) p &_sstack
    $7 = (<data variable, no debug info> *) 0x20000718
    (gdb) p &_estack
    $8 = (uint32_t *) 0x20000918
    (gdb) p &_sfixed
    $9 = (<text variable, no debug info> *) 0x8000000 <interrupt_vector>
    (gdb) p &_efixed
    $10 = (<text variable, no debug info> *) 0x8003790

    What is the expected memory layout? Is there a page for that?

    regards,
    -anand

    On Mon, May 4, 2015 at 1:58 PM, anand srivastava
    <[email protected] <mailto:[email protected]>> wrote:

        Hi Hauke,

        Thanks for the prompt response.

        I have

        arm-none-eabi-gcc (GNU Tools for ARM Embedded Processors)
        4.9.3 20150303 (release) [ARM/embedded-4_9-branch revision 221220]

        Open On-Chip Debugger 0.9.0-rc1-dev-00001-gabd7ad0
        (2015-04-25-11:22)

        I have checked the RX/TX pins several times now :-).

        Also the debugger should not connect at that point.

        I guess I should try with the older GCC.

        regards,
        -anand

        On Mon, May 4, 2015 at 1:45 PM, Hauke Petersen
        <[email protected]
        <mailto:[email protected]>> wrote:

            Hi,

            just checked, the example is running just fine for me. I
            am using:
            arm-none-eabi-gcc (GNU Tools for ARM Embedded Processors)
            4.8.4 20140725 (release) [ARM/embedded-4_8-branch
            and
            Open On-Chip Debugger 0.9.0-dev-00415-g2d4ae3f-dirty
            (2015-04-20-15:09)

            Did you cross the pins for your UART converter (TX stm
            board -> RX UART converter)?

            Otherwise it would be helpful if you could state the
            details on your toolchain and openocd version.

            Let's fix this!

            Cheers,
            Hauke




            On 04.05.2015 09:33, anand srivastava wrote:
            Hi All,

            I am trying to use Riot for an internal project.

            I have tested Riot on native. I am stuck on the
            STM32F0-Discovery, which I expected to be pretty stable.
            I have the latest code from the repository.

            I have flashed the STM32F0-Discovery board with make
            flash utility, based on the instructions given at
            
https://github.com/RIOT-OS/RIOT/wiki/Getting-started-with-STM32F%5B0%7C3%7C4%5Ddiscovery-boards

            I got the following output from openOCD, which seems
            normal enough to me.

            
/media/linux-space/anand/Work/IoT/riot/RIOT/dist/tools/openocd/openocd.sh
            flash
            ### Flashing Target ###
            Open On-Chip Debugger 0.9.0-rc1-dev-00001-gabd7ad0
            (2015-04-25-11:22)
            Licensed under GNU GPL v2
            For bug reports, read
            http://openocd.org/doc/doxygen/bugs.html
            Info : The selected transport took over low-level target
            control. The results might differ compared to plain JTAG/SWD
            adapter speed: 1000 kHz
            adapter_nsrst_delay: 100
            none separate
            srst_only separate srst_nogate srst_open_drain
            connect_deassert_srst
            Info : Unable to match requested speed 1000 kHz, using
            950 kHz
            Info : Unable to match requested speed 1000 kHz, using
            950 kHz
            Info : clock speed 950 kHz
            Info : STLINK v2 JTAG v14 API v2 SWIM v0 VID 0x0483 PID
            0x3748
            Info : using stlink api v2
            Info : Target voltage: 2.901302
            Info : stm32f0x.cpu: hardware has 4 breakpoints, 2
            watchpoints
                TargetName Type       Endian TapName            State
            --  ------------------ ---------- ------
            ------------------ ------------
             0* stm32f0x.cpu hla_target little stm32f0x.cpu       halted
            target state: halted
            target halted due to debug-request, current mode: Thread
            xPSR: 0xc1000000 pc: 0x0800020c msp: 0x20000b98
            target state: halted
            target halted due to debug-request, current mode: Thread
            xPSR: 0xc1000000 pc: 0x0800020c msp: 0x20000b98
            ** Programming Started **
            auto erase enabled
            Info : device id = 0x20006440
            Info : flash size = 64kbytes
            target state: halted
            target halted due to breakpoint, current mode: Thread
            xPSR: 0x61000000 pc: 0x2000003a msp: 0x20000b98
            wrote 15360 bytes from file
            
/media/linux-space/anand/Work/IoT/riot/RIOT/examples/hello-world/bin/stm32f0discovery/hello-world.hex
            in 0.900809s (16.652 KiB/s)
            ** Programming Finished **
            ** Verify Started **
            target state: halted
            target halted due to breakpoint, current mode: Thread
            xPSR: 0x61000000 pc: 0x2000002e msp: 0x20000b98
            verified 14808 bytes in 0.205989s (70.202 KiB/s)
            ** Verified OK **
            shutdown command invoked
            Done flashing

            The board seems to be stuck in reset_handler

            Reading symbols from
            
/media/linux-space/anand/Work/IoT/riot/RIOT/examples/hello-world/bin/stm32f0discovery/hello-world.elf...done.
            Remote debugging using :3333
            reset_handler ()
                at
            /media/linux-space/anand/Work/IoT/riot/RIOT/cpu/stm32f0/startup.c:61
            61   for (dst = &_srelocate; dst < &_erelocate; ) {
            (gdb) p dst
            $1 = <optimized out>

            The USB to Uart converter has been connected to the
            prescribed ports TX=PB6 RX=PB7 GND=GND, but is not
            getting any output, probably because the board is stuck.

            I am sure I am missing something pretty basic, but I have
            no clue as to what it is. The code looks proper enough.
            Thanks for any ideas on how to move ahead.

            regards,
            -anand




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