On Thursday 03 September 2015 11:24:34 Gene Heskett wrote:

> On Thursday 03 September 2015 07:50:59 Peter Blodow wrote:
> > Hello Gene,
> > I have beeen following your description of what you were doing to
> > you machinery for weeks now, but I must confess that I have lost
> > track on the way, can't imagine in most cases what you are
> > describing. How about mailing a couple of picture of your goodies so
> > I can re-read your mails and get an image of your "new" shop
> > equipment?
>
> I'll take my camera out with me today, and post some pix on my web
> page in the next day or so.
>
> I am quite likely guilty of switching the referenced machine in the
> word "the" in the middle of a sentence, and I'm sure that can be
> confusing.
>
> In re the lathes control box, has two 2M542 stepper drivers in it,
> with a 4" 12 volt computer fan blowing on the heat sinks of each one. 
> Power supply is a full wave bridge, choke input filter, with about 12k
> uf's filter caps.  To get operating voltage for the fans, an LM317 was
> setup to output about 17 volts, which spins the fans right up.  Then
> from that 17 volts, a 7805 makes 5 volts for the C1G BoB.  Because the
> sink tab on an LM317 is also the center, output terminal, and therefor
> electrically hot, I had mounted it with an insulator kit using the
> thin si rubber insulator.  No grease in deferrence to the si rubbers
> life expectancy.
>
> Bolted to half a square foot of 1/4" thick alu plate should have been
> enough heat sinking, but apparently was not, particularly when, in the
> process of putting a pcb on the outside of the box to carry a 5 pack
> of 5 pin, 2.54 spaced plugs so that everything could be unplugged if I
> needed to move the lathe out and work on it, but I misswired the plug
> for the encoder creating a short on the 5 volt line from the BoB.
> Fairly close to instant toast for the LM317.
>
> But it did work for a couple years until the dummy sitting in this
> chair screwed up.
>
> I thought that LM317 was the last one in local captivity and ordered
> some switching buck switchers from China but they are still 10 days
> away. So finding a bag of 8 or 9 LM317's will rescue me till they
> arrive.  Their improved efficiency will reduce the load on the motor
> supply transformer and should reduce the overall heat level in that
> box by at least 20 watts.  But this will do in the meantime.
>
> In the meantime I used the same pwm driven servo amp that Pico sells
> for the spindle motor driver in the new mill, so what I learn about
> using a limit3 to reduce the brutality of a motor reversal will get
> taken back to the lathe, where I have 50 lines of hal code and about 7
> code modules doing a much gentler reversal that results in several
> turns of overshoot from the position specified in the G33.1 command
> line. I added some more code to latch the spindles position when the
> motion module issued the reversal command, and when it had actually
> made a couple degrees of motion in the new direction.  With a 20 lb
> chuck, and doing a rigid tap at 300 rpms, the overtravel was just
> short of 3.5 full turns of the chuck.
>
> Even with the limit3 to soften the turnaround, the mill can do that
> same reversal and get back to full speed in about 1 second, at 2500
> rpms!
>
> So I am learning that A: Jons servo amp is one tough bit of gear, and
> B how to exploit it to do something that on the lathe would only have
> succeeded in burning up another of those plastic timing belt sprockets
> that I have probably burned up 20 of in the 15 years I had that piece
> of junk.  But now I have on hand, a new head, with all metal backgears
> in it, and a conversion kit to change the chinese belt out for the
> much taller cogs XL belt, but it came from fleabay with a very small
> tooth count, 10 I think, and bored for the 8mm OEM motor shaft, but I
> had made a jackshaft to replace that motor, driven by a 3" polygroove
> pulley from the nominally 1" pulley on a treadmill motor. So I bought
> some 16 coggers with a 10mm bore to replace the 10 cogger that boring
> to 9mm destroyed, so now I need to make a new jackshaft with a 10mm
> nose for these sprockets.  And I may have to order a longer XL belt if
> I can't lift the jackshaft enough to make this one fit.  Realisticly,
> milling some off the top of the jackshaft frame would be quicker than
> obtaining the longer belt.
>
> On top of all that, the treadmill motor has now developed a rumble
> that says the load end bearing on the armature now has square balls in
> it. And the flywheel/fan/pulley I will have to remove to gain access
> for replacing it, is superglued to the motor shaft as its not a keyed
> drive, but screwed to the shaft, self tightening in the treadmill use,
> but I'm turning both ways so I glued it on.  I hope I can get it hot
> enough to make the glue release. I noted yesterday that the fan has
> some wobble I had not noticed before, so its possible the shaft itself
> is bent, those polygrove belts don't slip when the chuck make a stop
> in about 2 degrees of rotation because the toolpost has tipped the
> whole carriage into the work, digging a ramp about 100 thou deep as it
> tips and stopping it in about 10 degrees of motor shaft rotation from
> 4000 rpms.  That this rumble started after the last such instance is
> clue #2.
>
> The fix for that is to swap the rubber compound assembly for a 2x2x4
> block of steel, which will allow me to bore the QC holders 10mm
> holddown bolthole at the right rear of the block, which in turn will
> place the cutting forces on the middle of the carriage as opposed to
> hanging off the front, making the right edge of the carriage lift a
> thou, tipping the tool into the work to start the the whole show all
> over again.
>
> Or a new lathe big enough to do what I ask this one to do.  But the
> shops 2 layers of OSB flooring wouldn't handle that weight without
> picking it up and pouring a concrete slab under it.
>
> Now theres a word picture for you. :)
>
> That has me scanning fleabay for another motor, and becoming resigned
> to remaking the mount to the jackshaft.  Sigh.
>
> As Guilda Radner was fond of saying, its always something...
>
> I'll get some newer pix & post them over the next 2-3 days.

Mid afternoon PS:  The LM317T is in and working, but that 1.75x3.5" bit 
of 1/8" alu for a heat sink is running just under 150F after about 20 
minutes running. The draw of a 3rd fan will also make it run even 
hotter, so there is a point of vanishing returns to such thoughts. I may 
have to add a 3rd fan, but have no clue what to hang it from. It will  
no doubt get more air with the lid closed, spillage from the end of the 
X motor driver.

The theory was when I built that box was to have enough air moving inside 
it to carry the heat to the outside walls for normal radiant cooling.

That way, flying swarf stands a very small chance of ever entering the 
box.  Its also sitting on a 5 foot tall wooden chest of drawers I made 
for a toolbox about 15 years ago, and about 18 inches above the lathes 
centerline.  Swarf gets up there by way of the air hose when I am 
cleaning up but not otherwise.

Its sitting out there smoke testing, but has not been "run the lathe" 
tested yet.  Thats about an hour away. :)

Cheers, Gene Heskett
-- 
"There are four boxes to be used in defense of liberty:
 soap, ballot, jury, and ammo. Please use in that order."
-Ed Howdershelt (Author)
Genes Web page <http://geneslinuxbox.net:6309/gene>

------------------------------------------------------------------------------
Monitor Your Dynamic Infrastructure at Any Scale With Datadog!
Get real-time metrics from all of your servers, apps and tools
in one place.
SourceForge users - Click here to start your Free Trial of Datadog now!
http://pubads.g.doubleclick.net/gampad/clk?id=241902991&iu=/4140
_______________________________________________
Emc-users mailing list
[email protected]
https://lists.sourceforge.net/lists/listinfo/emc-users

Reply via email to