this sounds a lot like the problem I had with my Porsche hub which I made on
my raggedy lathe. it was out 15/1000 on the dial indictor which means out
7.5/1000 as the high and low add .  It turned out to be the key was to big
and when I filed it down the hub came to 5/1000 on dial or 2.5/1000 . I had
been thinking of getting rid of the clutch/presser plate and flywheel  and
using a lov joy coupler as is in my work truck .  How big is the shaft ?
Have you tried bolting it together 180* from were its at .
Snip >  I put the runout gauge on the flywheel, and measured almost
> 40/1000's runout on the flywheel.
 I think this means 20 /1000 out which is to much
I will be very interested to see what others say about this  as I have just
gone through it . I have not had to chance to rev it up since I fixed it
  ----- Original Message -----
From: <[EMAIL PROTECTED]>
To: <[EMAIL PROTECTED]>
Sent: Wednesday, August 21, 2002 10:38 AM
Subject: Vibration, and the undocumented science of adapter design


> Slowly wrapping up the conversion of a 99 Ranger to electric, using
> Metricmind's AC drive system.
>
> The first time the truck was assembled it had a noticeble vibration
> whenever the motor was spun, even with the transmission out of gear.  I
> didn't think it was too severe and drove the truck for a few days.  A
> missed shift caused me to accidentially spin the motor to its rev limit at
> 7000rpm, and quite suddenly the vibration got a lot worse.
>
> Disassembly of the adapter showed the 4" long motor shaft to be bent
> (almost 40/1000's of an inch).  Also I found several noticible gashes on
> the inside of the bell housing, and the clutch slave cylinder thrust
> bearing had cut a groove into its shaft.
>
> Took the motor apart and sent the rotor/shaft to a propeller machinist.
> He used a tool meant for straightening bent prop shafts, and brought the
> motor shaft to within 3/1000's of true again.  So now I am putting
> everything back together, and taking extra care to balance and true
> everything.
>
> Here's my problem.  The face of the hub attached to the motor shaft is
> perpendicular to the rotation of the shaft to within about 2/1000's of an
> inch and the centering ring is concentric.  Spin just the hub up to 7000
> RPM, everything is smooth, no vibration.  I attached the flywheel and
> pressure plate (which were professionally balanced) and the whole system
> gets a scary vibration, shaking the truck noticibly before even getting it
> to 3000RPM.  I put the runout gauge on the flywheel, and measured almost
> 40/1000's runout on the flywheel.
>
> Figuring the flywheel warped (it had been lightened to about 1/2 thick) I
> replaced it, had the new flywheel resurfaced and balanced... same problem,
> the face is out of true by about 40/1000's and it vibrates heavily.
> Unfortunetly I have not been able to have the balance shop do the
> hub/flywheel/pressure plate together, becuase his balancing arbor won't
> fit inside the splined portion of the hub (the Siemens motor has a splined
> shaft)
>
> Some possible thoughts:
> 1. The Siemens motor has a shaft almost 4" long, with the hub attached to
> that, and the flywheel hanging about 1/2 beyond the end of the shaft.
> Victor says the motor shaft should have no issue with 20lbs of flywheel 4"
> from the motor bearing, but the shaft has bent once already for unknown
> reasons, and everyone who looks at it gets nervous.
>
> 2. The balancer isn't balancing, or the machinist that resurfaces the
> flywheel isn't verifying that the front and rear faces are perfectly
> parallel.
>
> Any other ideas?  Is 40/1000's acceptable for a flywheel face?  Should I
> shop around for a balancer with a smaller arbor on his machine?  Or make
> an adapter that would convert from the spline to something an arbor could
> grab?
>
> Thanks
> Mark Farver
> Austin, Texas
>
>

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