Day 4 - Crofton to Great Bedwyn
The day dawned with weather more appropriate to Peasedown St John  
than Crofton and it continued to rain on-and-off though the morning.   
So we faffed about - Lynne sewing and Baz trying to siphon oil out of  
the gearbox [with limited success - chalked up as a partial oil  
change].  Less rain after lunch so we pushed off for a gentle potter  
eastwards.  Waited after Lock 61 for nb Forget-me-Not to catch up and  
then waited some more at Lock 62 for a crazy couple to get a cruiser  
into the lock without pirouetting in the wind too often.  Waited for  
an up-coming boat at lock 63 and lost further time at Lock 64 while  
it filled on one paddle.  In the end a trip that my 'ready- 
reckoner' [computed from previous logs] should take 1.25 hrs took 2  
hrs.  However, we were in no hurry and had plenty of time to find a  
mooring beyond the VMs.  As we arrived a bizarre rattling sound came  
from the engine - proved eventually to be the air filter element in  
which the foam had separated from the expanded metal fastening and  
the filter housing had thus been turned into an effective random  
sound generator.  I expect it was designed by Lister to do that to  
remind me to change it - 1,500 hrs is probably enough.  All we had to  
do then was eat, pack up all the valuables and catch a train back to  
Bradford-on-Avon to collect the car so we could wend homewards.
Distance: 1m 6fl; Locks 4; Engine hours: 2.01

Reports resume at the weekend, hopefully.

Baz

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