Here are some cooling ideas
- Factory baffles are dreadful however new ones can easily be made out of 1mm 
Al sheet. Note where the old ones are inadequate and then use them as templates.
- Follow Macca's advice and become obsessive/compulsive about sealing air gaps 
with silicone and aluminium tape.
- Fit some decent baffles under the barrels next time you have the
heads off - the VW people have ones for 1600 motors that require only minor
modification. I think the ones from limbach that Nigel can get may not require 
the heads to be off to fit them.
- Make sure the rubber seals are making good contact with the cowl and are in 
good condition.   

While I am at it.... check that the prop change fork contacts the prop evenly. 
All three of the H36's that Nigel and I did up were way out with one bearing 
loading up the prop plate way before the other. I suspect this as being a 
factor in breaking studs.

cheers
Rob Thompson


 PO Box 129,
Lawson, NSW, 2783.
mobile 0429 493828


























.............................................




________________________________
From: Ian Williams <[email protected]>
To: [email protected]
Sent: Tue, 29 December, 2009 8:26:35 AM
Subject: RE: [DOG mailing list] hk36 crash

 
Hi Ian,
 
My view (for what it is worth) is that over the years there has
been less and less practical blokes coming along, and more and more who think
that high powered engineering takes place behind a computer screen. Resulting
in the thought that things get fixed or sorted out by divine intervention only
 
While not a H-36,  our little Grob 109A has just blasted
skywards with its Limbach L2400 engine.  (it does have a H-36 designed
pitch change fork though) so that should be OK for the DOG list.
 
Actually ... the take off performance is improved significantly
of course but the top end is much the same.
 
I did spend a lot of time static balancing the Prop
....   (had to load up one side of the prop hub with an astounding
amount of metal to get it right)  but the effect was incredible ... real
smooth. Also got rid of a 2mm thrust plate run out 
 
It would seem that crappy engine baffles, real bad cooling exit
design and an out of balance prop all conspired to screw the original  L2000
engine before it got to 500 hrs.  It had a 3rd cracked case .
 
Maybe engineers have a bit to answer to as well..!!
 
 
Best regards
 
Ian Williams
 
 
From:Ian Mc Phee [mailto:[email protected]] 
Sent: Monday, 28 December 2009 11:18 p.m.
To: [email protected]
Subject: Re: [DOG mailing list] hk36 crash
 
It seems that JB did not listen to Lewis Zurgen (was rude to
Lewis when he tried to help) the original owner of hk36 GXD and he is the one
that put in the accumulator solenoid for a real reason to hold pressure in
system after a long soaring flight so as to unfeather prop and thus pilot had
little chance of learning and pilot did not have an understanding of Bings and
throttle setting for start.
 
I am afraid there are people out there who can pass a flight
test but not really understand why they are doing a certain proceedure
 
Another example is taxiing out with electric fuel pump OFF
(which checks mechanical) and then ele pump ON just before rolling.  JB
just left it ON - am I too fussy or is that not done anymore?  
 
Ian M 
  
2009/12/28 Rob Thompson <[email protected]>
Ian
mentions that the pilots of the crashed HK36 didn't have an understanding of
some of the engine systems....Can anyone explain to me how they got a type
endorsement with out knowing this?

Rob
 
PO Box 129,
Lawson, NSW, 2783.
mobile 0429 493828


















 
.............................................
 
 
No virus
found in this incoming message.
Checked by AVG - www.avg.com
Version: 8.5.431 / Virus Database: 270.14.122/2590 - Release Date: 12/28/09
07:16:00


      
__________________________________________________________________________________
See what's on at the movies in your area. Find out now: 
http://au.movies.yahoo.com/session-times/

Reply via email to