Le 2014-02-19 22:24, Frederic RIBLE a écrit :
> Le 2014-02-16 21:32, Frederic Rible a écrit :
>> Michael, thanks.
>> Here is some more detail.
>>
>> I am running pre0.5184
>> My config is here:
>> http://blog.f1oat.org/wp-content/uploads/2013/11/CNC-6040-2014-02-16.tar.gz
>>
>> And the output of linuxcnctop below.
>> Frederic.
>>
>> acceleration 1e+99
>> active_queue 1
>> actual_position      633.0000 410.0000 92.0000  0.0000
>> adaptive_feed_enabled        0
>> ain  0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0
>> 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0
>> 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0
>> 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0
>> angular_units        1.0000
>> aout 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0
>> 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0
>> 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0
>> 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0
>> axes 4
>> axis_mask    15
>> block_delete 0
>> command      G0 X320
>> current_line 0
>> current_vel  0.0000
>> cycle_time   0.00098865
>> debug        0
>> delay_left   0.0
>> din  0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0
>> 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0
>> distance_to_go       4.0801
>> dout 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0
>> 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0
>> dtg  -4.0801  0.0000   0.0000   0.0000
>> echo_serial_number   5
>> enabled      1
>> estop        0
>> exec_state   done
>> feed_hold_enabled    1
>> feed_override_enabled        1
>> feedrate     1.0
>> file /home/f1oat/linuxcnc/configs/CNC-6040/nc_files/axis.ngc
>> flood        0
>> g5x_index    1
>> g5x_offset   308.9199 170.0000 92.0000  0.0000
>> g92_offset   0.0000   0.0000   0.0000   0.0000
>> gcodes       G0 G17 G40 G21 G90 G94 G54 G49 G99 G64 G97 G91.1 G8
>> homed        1 1 1 1
>> id   0
>> inpos        0
>> input_timeout        0
>> interp_state reading
>> interpreter_errcode  0
>> kinematics_type      identity
>> limit        0 0 0 0
>> linear_units 1.0000
>> lube 1
>> lube_level   0
>> max_acceleration     1e+99
>> max_velocity 0.0000
>> mcodes       M5 M9 M48 M53 M0
>> mist 0
>> motion_line  0
>> motion_mode  coord
>> motion_type  traverse
>> optional_stop        0
>> paused       0
>> pocket_prepped       -1
>> position     633.0000 410.0000 92.0000  0.0000
>> probe_tripped        0
>> probe_val    0
>> probed_position      0.0000   0.0000   0.0000   0.0000
>> probing      0
>> program_units        mm
>> queue        1
>> queue_full   0
>> queued_mdi_commands  0
>> read_line    0
>> rotation_xy  0.0000
>> settings     0.0 0.0 0.0
>> spindle_brake        1
>> spindle_direction    0
>> spindle_enabled      0
>> spindle_increasing   0
>> spindle_override_enabled     1
>> spindle_speed        0.0
>> spindlerate  1.0
>> state        rcs_exec
>> task_mode    mdi
>> task_paused  0
>> task_state   on
>> tool_in_spindle      0
>> tool_offset  0.0000   0.0000   0.0000   0.0000
>> velocity     0.0
>>
>>
>>
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> Very strange.
> I have pulled the last master release source code, compiled it and run
> in place.
> Everything seems ok.
> I do not understand why I have regression issues with last buildbot
> packages.
> May be something in my environment that is not compatible with recent
> automatic builds.
> I continue my analysis.
> Frederic.
>
>
>
>
>
>
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I am now running pre0.5189
One clue: I have tested with default configurations coming with the 
lucid package.
* sim/axis : ok
* sim/gscreen : ok
* sim/gmoccapy : MDI stucked
I believe I am not far from understanding the root cause !
Stay tuned.
Frederic.




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