On 5/7/23 05:49, andy pugh wrote:
On Sun, 7 May 2023 at 08:35, gene heskett <ghesk...@shentel.net> wrote:

I have a need for a refresher course on the proper usage of the new
at-pid module now used in master. I've some nasty problems with it and
the accuracy of my machines that use it has gone to the dogs, hunting
and drifting when supposedly still.  If it can't be solved, I'll have to
rip them out and put stepper/servos on this go704 at around $250/axis.


I would suggest that the first thing to do would be to step back to 2.8 and
see if the issues you see disappear.

Unless you actively engage auto-tune mode the component should behave the
same as it always did.

Have you changed the PID settings at all since your machine was working
properly?

yes, considerably. The previous settings were more like WAG's that worked. But see my other later post, I wasn't following ALL the instructions. My bad IOW.

Take care & stay well Andy.

Cheers, Gene Heskett.
--
"There are four boxes to be used in defense of liberty:
 soap, ballot, jury, and ammo. Please use in that order."
-Ed Howdershelt (Author, 1940)
If we desire respect for the law, we must first make the law respectable.
 - Louis D. Brandeis
Genes Web page <http://geneslinuxbox.net:6309/>



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