Heinz Reimer, Thanks for the input. I will check into the information you provided. Seems a shame thought to have to use a counter weight on Z axis as the system should have been designed to move it own weight. If you have any pictures on the counter weight you used please send them to me.
John Domville -----Original Message----- From: Heinz Reimer [mailto:[EMAIL PROTECTED] Sent: Saturday, November 01, 2008 10:57 PM To: Enhanced Machine Controller (EMC) Subject: Re: [Emc-users] Engrave-11 Z test at 50 percent [EMAIL PROTECTED] wrote: > Ok... > Test one , with the delay/pause ran flauless. ( at 50 % feed over ride) > > Part two ( with out the delay/pause) had problems. It made a couple of cycles then started the "binding noise" again, on both the up and down movement of the Z axis. The tool did not stay .500 from the table but moved closer and closer until I terminated the program manually . Both tests were run with the AXIS slide bar for FEED OVERIDE at 50%. So where in the config do I cjhange what? > > On the main " Driver page" I have the following settings: > > Step Time 5000 > Step Space 5000 > Direction Hold 20000 > Direction Step 20000 > > and on each one of axis pages there is the following settings" > > Motor Steps per rev 200 > Driver Micro Stepping 4.0 > Max Velocity 1.0 in/sec > Max Acceleration 30.0 in/sec. > > John > > ------------------------------------------------------------------------- This SF.Net email is sponsored by the Moblin Your Move Developer's challenge Build the coolest Linux based applications with Moblin SDK & win great prizes Grand prize is a trip for two to an Open Source event anywhere in the world http://moblin-contest.org/redirect.php?banner_id=100&url=/ _______________________________________________ Emc-users mailing list [email protected] https://lists.sourceforge.net/lists/listinfo/emc-users
