Well I just got done taking the 140 out for about a mile long cruise. Smoke all cleared out as far as I could tell in the almost dark. Engine ran great, had plenty of power etc, tranny shifted fine which it did before. The only major thing now is it seems to have developed quite a vibration. Im thinking maybe its from the tires since its been sitting?? The tires are just about brand new before I started working on the car. It was smooth down the road before. I dont see that there would be a driveshaft problem, it went back together the same as I took it apart. I will have to investigate that further. If it is from the tires sitting, will that go away after a while on its own?

On 1/9/2011 12:14 PM, Kaleb C. Striplin wrote:
I think I am about ready to call it done, I got all the misc crap such as covers and what not in the engine compartment. I think I got that oil leak from the turbo return fixed. I used a prybar and bent the tube a little bit so it seems straighter now. I did run it up to operating temp yesterday and did start and run it this morning to see if it was still leaking oil. A couple of things I have observed. When stone cold it fires up and idles smooth. After a minute with the afterglow turns off it does seem to idle a little rougher and maybe miss on occasion and smoke more. After a few minutes of this and the engine is warmed it idles smooth again. Im hoping this is a condition that goes away after the engine is run a bit and cleaned up. I used some JB weld to plug up that broke off nipple on the main vacuum line, once it sets up Im going to pull the car out of the garage and take it up and down the street and see if she flys apart or not. I am quite sure once I put the wife back in it something will blow up.

On 1/8/2011 6:02 PM, Kaleb C. Striplin wrote:
the brand new glow plug wiring harness arrived from Rusty yesterday so today I put it on and put the intake etc back on (made MUCH easier by my purchase of HF allen T wrenches. Still no glow plug light. I stole the one off my 91 350SDL and it glows and starts fine. I guess maybe the shorting out fried the old relay. I tell you having never messed with pulling heads, replacing rods etc I am sure nervous the whole thing will fly apart. BTW, this is the engine I just replaced the #1 rod with the updated heavier rod. Just from my observation I dont sense any different vibrations even though the weight does not match the other rods. Will see what time holds for it though.


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Kaleb C. Striplin/Claremore, OK
 95 E300, 94 S500, 92 500SEL, 92 300SD, 92 300E 4Matic,
 91 350SDL, 91 300D, 89 560SEL, 87 300SDL x2, 85 380SE 5.0 Euro,
 85 190D, 84 190D, 84 300D euro manny, 76 240D, 76 300D,
http://www.okiebenz.com


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