Thank you! If possible, could you please give me more detailed instruction on how to solve this? Maybe some links would be very helpful!
On Monday, May 6, 2019 at 5:09:27 AM UTC-7, ithinu wrote: > > It was something like new OS on an sd card, but something outdated in the > booting sequence on the EEPROM and I needed to fill the latter with > zeros... something strange like that if I remember well. > > On Monday, May 6, 2019 at 1:58:10 PM UTC+2, [email protected] wrote: >> >> Hello, I have the same problem here so I cannot run on boot either. Have >> you solved this problem? >> I'm looking forward to hearing from you, thank you! >> >> On Monday, January 14, 2019 at 5:21:43 AM UTC-8, [email protected] wrote: >>> >>> I use >>> http://strawsondesign.com/docs/images/BBB-blank-debian-9.5-iot-armhf-2018-10-07-4gb.img.xz >>> >>> from http://strawsondesign.com/docs/librobotcontrol/flashing.html. I >>> flashed it into the built-in eMMc as the page told that it is better so. >>> >>> Then I configured librobotcontrol to use rc_balance as told here >>> http://strawsondesign.com/#!edumip-software, which gave an error: >>> >>> $ systemctl status robotcontrol.service >>> ● robotcontrol.service - robotcontrol >>> Loaded: loaded (/lib/systemd/system/robotcontrol.service; enabled; >>> vendor preset: enabled) >>> Active: failed (Result: exit-code) since Sun 2018-10-07 16:42:07 UTC; >>> 13s ago >>> Process: 1278 ExecStartPre=/usr/bin/rc_startup_routine (code=exited, >>> status=255) >>> >>> Oct 07 16:42:06 beaglebone systemd[1]: Starting robotcontrol... >>> Oct 07 16:42:07 beaglebone rc_startup_routine[1278]: timeout reached >>> while waiting for pwm driver >>> Oct 07 16:42:07 beaglebone rc_startup_routine[1278]: TIMEOUT REACHED >>> Oct 07 16:42:07 beaglebone systemd[1]: robotcontrol.service: Control >>> process exited, code=exited status=255 >>> Oct 07 16:42:07 beaglebone systemd[1]: Failed to start robotcontrol. >>> Oct 07 16:42:07 beaglebone systemd[1]: robotcontrol.service: Unit >>> entered failed state. >>> Oct 07 16:42:07 beaglebone systemd[1]: robotcontrol.service: Failed with >>> result 'exit-code'. >>> >>> $ uname -a >>> Linux beaglebone 4.14.71-ti-r80 #1 SMP PREEMPT Fri Oct 5 23:50:11 UTC >>> 2018 armv7l GNU/Linux >>> >>> I guess the hardware is ok, as I previously used some old image from >>> https://www.hackster.io/edumip/edumip-13a29c and rc_balance was fine. >>> >>> -- For more options, visit http://beagleboard.org/discuss --- You received this message because you are subscribed to the Google Groups "BeagleBoard" group. To unsubscribe from this group and stop receiving emails from it, send an email to [email protected]. To view this discussion on the web visit https://groups.google.com/d/msgid/beagleboard/c0127e8c-8747-4267-a020-c15c02785d47%40googlegroups.com. For more options, visit https://groups.google.com/d/optout.
