I had pretty decent luck torqueing the keel bolts today.  A few of the
studs were damaged/corroded on the threads extending past the nut but not
on the threads protected by the nut when fully tightened.  I lubed the
rough threads with extra thick tef-gel and things seemed to go together
smooth enough.  The 3:1 multiplier was effective but I think a 4:1 or 5:1
would have made the job a little easier.  I was definitely glad I brought a
3 foot pipe to help stabilize the reaction bar.  It was extremely helpful
to have a second person present to monitor and stabilize the whole
apparatus.  I stand by my statement from last night that keeping the
operating wrench as close to the multiplier as possible minimizes the
creation of odd twisting motions.  My concerns of using an output drive
extension were unfounded and I would encourage anyone who is hesitating, to
use one.

We were out of the water and set on a block around 9:30am and done with the
torque by 12:30.  This included removing each nut, cleaning the nut and
stud, and then reinstalling each one at a time.  Overall a very smooth
process but the preparation was a very important part.

I used the torque values from the link below as a guide.  316 SS
lubricated.

https://www.fastenal.com/content/feds/pdf/Torque%20of%20Stainless%20Steel,%20Non%20ferrous%20Torque.pdf

Keel bolts (fwd to aft):
         Nut                       stud               torque        3:1
multiplier
1 - 1 1/2 (38mm)    1 (25mm)          255 =          85 x 3
2 - 2 3/16 (56mm)  1 1/2 (38mm)  615 =          205 x 3
3 - 2 3/16 (56mm)  1 1/2 (38mm)  615 =          205 x 3
4 - 2 3/16 (56mm)  1 1/2 (38mm)  615 =          205 x 3
5 - 1 7/8 (47.5mm)1 1/4 (32mm)   465 =          155 x 3
6 - 2 3/16 (56mm)  1 1/2 (38mm)  615 =          205 x 3
7 - 1 1/2 (38mm)    1 (25mm)          255 =          85 x 3
8 - 3/4 (19.5mm)    1/2 (13mm)      38

Josh Muckley
S/V Sea Hawk
1989 C&C 37+
Solomons, MD



On Jan 2, 2018 3:18 PM, "Josh Muckley via CnC-List" <[email protected]>
wrote:

Ok Guys,
Since I have the mast out, this provides the rare opportunity to access ALL
of the keel bolts.  I've measured each of the bolt and nut diameters and
checked the archives for torque specs.  I intend to buy a toque multiplier
and the appropriate sized sockets.  I think I can do it for less than the
yard is going to charge and I'll come out of it with some tools.  I'll also
be able to tell myself that it was done correctly.

That being said it sounds like the best practices are are follows:
-  be on the hard
- loosen the bolts one at a time, clean, and lubricate with tef-gel
- reinstall and torque at progressively higher levels.

I was unable to find the torque spec for my 1.5" bolt in the website but
Ken Heaton cited 600lbs in one of his past responses.

Keel bolts (fwd to aft):
         Nut                       stud               torque
1 - 1 1/2 (38mm)    1 (25mm)          350
2 - 2 3/16 (56mm)  1 1/2 (38mm)  600?
3 - 2 3/16 (56mm)  1 1/2 (38mm)  600?
4 - 2 3/16 (56mm)  1 1/2 (38mm)  600?
5 - 1 7/8 (47.5mm)1 1/4 (32mm)   450
6 - 2 3/16 (56mm)  1 1/2 (38mm)  600?
7 - 1 1/2 (38mm)    1 (25mm)          350
8 - 3/4 (19.5mm)    1/2 (13mm)      80


*Anything I'm missing?*


Thanks,

Josh Muckley
S/V Sea Hawk
1989 C&C 37+
Solomons, MD

_______________________________________________

Thanks everyone for supporting this list with your contributions.  Each and
every one is greatly appreciated.  If you want to support the list - use
PayPal to send contribution --   https://www.paypal.me/stumurray
_______________________________________________

Thanks everyone for supporting this list with your contributions.  Each and 
every one is greatly appreciated.  If you want to support the list - use PayPal 
to send contribution --   https://www.paypal.me/stumurray

Reply via email to