On 6/2/2012 2:14 PM, Dave wrote:
> Unfortunately if he buys a transformer it still might not work. That 
> is why I would try and borrow one before opening my wallet for $1400. 
I hope to borrow one before dumping more cash into this machine, as 
stiff as the phase converter is not I'm wondering if the infeed unit is 
weak... I did notice that my feed from the breaker panel to the RPC 
panel was a bit on the small side so I'll up the gauge on that as I have 
some 6 gauge SO cord laying about and see what that might do.

>>> The higher the %, the more voltage drop through the
>>> transformer/reactor.   So what John was saying is that the 611 system
>>> can use up to a 3% reactor, but no more.
>>>
>> Can I assume then that when the BBLB syndrome is accounted for, that a 3%
>> transformer is probably going to cost 50% more than the one yonder on the
>> shelf that sells for 1.4G's or less in the size John needs?
>>
>>
>>> Meaning the 611
>>> expects a very stiff power supply, which really does not surprise me as
>>> it is a rather high performance drive system.  Most of the machines
>>> equipped with 611s that I have seen are serious industrial machines
>>> where there is a 1000 amp 480 volt bus duct 50 feet from the machine,
>>> etc.
>>>
>> Well, at some point it should become a discussion where the cost of
>> switching the drives out for something that can tolerate a softer regulated
>> power supply source is becoming one possible solution. I expect that Johns
>> location, way off the main line, will account for the first 1.5% of that 3%
>> budget.  Thats item 1.  Item 2 is the cost, and the 24/7 power used to
>> power a ferroresonant regulator such as a Sola that big is a measurable
>> percentage of his monthly power bill. They run HOT, he could heat the shop
>> with it in cooler weather.  But unlike the fans and/or AC, you can't turn
>> them off when you don't need the heat.  They are also frequency sensitive,
>> enough so that driving it from the diesel generator is out unless it has a
>> .5% governor and double the size needed.
>>
>> Those drives in that size range obviously aren't cheap.  IMO, I'd be
>> looking for parts to take his raw single phase, working into a full wave
>> bridge rectifier, with a serious choke to maintain the power factor to
>> something reasonable, and feed that into a switchmode regulator whose
>> output was the 600 volt DC bus the rest of it needs.  With proper design it
>> is at least as efficient as the 60 HZ transformer, as its transformer is
>> ferrite cored and running at 30 kilohertz, and probably moreso, and could
>> hold that 600 volt buss at 600 with 0.01% regulation despite the startup
>> sags it would impose on the input line.  And it shouldn't cost, if such a
>> beast is even available, any more than one of those 611 drives.
>>
>>
> The 611 infeed/power supply has a ribbon cable connection to the rest of
> the drive bus and it communicates with the other modules, so it is very
> much a smart drive system.   If would be a major effort to make up a new
> infeed unit and create the control signals to keep the rest of the
> modules happy.  The communications on the ribbon cable is proprietary.
I assumed that the ribbon cable did this...
>
> So the availability of such a beast might be the controlling factor.
>> One thing is for sure Dave, if I was 50 years younger and contemplating the
>> purchase of a machine that had these drives it it, I would certainly
>> discount my bid by the amount of headache this thread has become to John.
>>
> Bigger used 3 phase CNC machines oftentimes go for a lot less money than
> slightly smaller CNC machines that run of single phase and this is
> why.   It has been a while, but I got the impression that John got that
> machine at a very good price.
>
I paid $6k plus delivery about $750 or so and have about $3.5k in 
tooling for the beast...
>> But that is the advantage of hindsight.  ;-)  What we need to do now is
>> find a solution that Just Works(TM).  The use of the limit2 module
>> functioning as a digital miller integrator to control the start up speed
>> ramp up, and the delta/wye isolation transformer, which will add its 3 or
>> 4% to the mix, might be the best solution for John.  How that will fare if
>> a big inch face mill is installed remains to be determined.
>>
>> Cheers, Gene
>>
>
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