Hi, Norm,  and list,

I didn't have to do what you did in my recent disassembly of my KISS, but I 
have a couple of addenda.

First is that separation of the rotor and stator is very straightforward. 
Just take a rubber or wood mallet and tap from the rear downward with the 
rotor stood on something other than your fiberglass deck :{))  Be ready to 
catch it as it separates.  No biggie at all.

The bearings go into silicon or some similar bushings which are made from a 
single strip, jam fit into receivers on the fin and nose ends.  Those strips 
are tapered to help center the of-necessity off-centered (clinging to the 
stator with its monster magnets) rotor.  They CAN come out, as my nose 
bearing did.  If you're going to have it apart, put in new - SVHotwire.com 
(John and Libbie at the show) sells them inexpensively - as they can wear 
from vibration, and work out of the receiver

My reassembly involved drilling out stripped-out helicoils (three of them - 
don't know if the factory is now using helicoils to resolve the stripping 
you experienced - had pulled away from the fiberglass housing) receivers, 
filling with fiberglass epoxy resin (I used West System), drilling out for a 
tap, and tapping the new holes.  If you had 10-24 helicoils, you could 
retrofit those if yours didn't have them originally, but solid epoxy, 
drilled and tapped is good, too.  I used the stator as my centering tool.

SVHotwire.com sells phillips headed bolt replacements in case you got tired 
of having the bit slip off the factory flat-blade tops :{))  Reassembly is 
the reverse - get the stator in position, held by loose fitted bolts, tap 
the rotor into the rear receiver.  Remove the bolts and put on the nose in 
the same fashion - tap with a soft hammer until the receiver catches and 
centers the bearing.  If you're going to remove it, spend a couple of bucks 
and get a new seal for the housing, too.  Grease liberally - there's a weep 
hole at the front of the housing which will express excess grease, but you 
want not to get any water in there if you can help it; the grease will help 
keep it out.

Mine didn't have a rubber gasket - instead Hotwire recommends GE silicone II 
sealant (as you said, do that before tightening the bolts).  Tighten it down 
very gently, let it sit for a couple of days to firm up and then tighten 
fully to give a gasket effect, wait a few days to fully cure, trim overrun 
if you want a really clean look, and back out the bolts until you can also 
seal those.  Done...

Second is balancing the prop.  I used to be model airplaner with 20k+ RPM 
engines and so had some experience in balancing props.  KISS should come 
with a balancing spindle, a specially threaded and tapered job.  I had one, 
but for the life of me can't find it so ordered another from John - $15 bux. 
The best $15 I have spent on this boat, but only because I followed up with 
absolutely anal balancing.

It was occasioned by my blades failing, so I had a new set of blades to work 
with.  Supposedly balanced at the factory, that's only static - they weigh 
the same, but the dynamic balancing is altogether different.  I wound up 
having to add weight to one blade and remove from two.  The lead strips 
attached to the blades are also available from Hotwire, in case you need to 
start over.

Just in case the mechanism of this isn't apparent to those not endowed with 
my history, I'll expand a bit, trying to be SOMEWHERE close to the 
instructive level of Norm :{))

The spindle has ~1/4" ends about 3/4" long - those are your axle.  If you 
had a stationary shop, you could do better than I - my prop rig was two 
straight razor edges far enough apart for the prop, and set perfectly 
level - and use a couple of steel straightedges (again perfectly level) set 
on two benches the appropriate distance apart, or you could use a vice with 
a wide enough throat and long enough width, though that wouldn't allow full 
rotation, for your axle seats. Screw the spindle in firmly (to avoid wobble) 
and commence balancing.

In my case, I used a fiddle on the workbench, reasonably level, and a large 
screwdriver, held eyeballed at "level" in both the axle and prop planes.  I 
didn't think fast enough.  I had a level in my tools which would have done a 
better job :{))  In any case, the axle ends were then free to rotate easily 
on a hard surface.  With the size of the prop (5' diameter), the very small 
axle made for very easy movement with any imbalance.

I commenced to balancing, and didn't have a clue about how much of the lead 
tape to cut off on each so I started gingerly.  Once I saw that 1/4" strips 
didn't have much effect, I got a bit bolder, and as I realized that one was 
significantly lighter than the other two, rather than remove the majority of 
lead strip from the two, I started taking bigger hunks from the heavier and 
applying them to the single lighter one.  Each time I did this process, I 
started with the lightened blade horizontal.  If I'd taken too much, it 
would rise.  If too little, it would fall.  Rinse, repeat - in my case, for 
a total, probably, of 10 hours at the end, occasioned by having to remove 
the prop and trim the tape, and then get it all lined up again before I 
recommenced the balancing.  The lightened ones never rose - I just kept 
repeating until I got to the end...  Back to the story...

Eventually I got to the point where the blade was rotating slowly, rather 
than falling like a stone.  I then started nibbling, doing max 1/4, but 
most, as I got closer, 1/8" or less.  (When I was doing model airplane 
props, it was sanding a little at the end, after I'd used a razor knife to 
shorten in the big steps.).  The lead strip is adhered such that a careful 
cut with a razor knife will allow you to peel off the adjustment easily. As 
mentioned, in the beginning, I reused those longer - 1" down to 1/2" - 
strips to weight the light blade.  If you want to do something like that, 
just be very careful of the adhesive when you handle it and where you stick 
it until you reuse it.  Doing it that way meant that I took off 
substantially less on the heavy blades than I'd have had to if not weighting 
the light blade.

Eventually, it took a full minute for the heavy blade to rotate from 
horizontal to vertical, in both directions, and moving my screwdriver ~10* 
from level easily made it rotate downhill in whichever direction I moved it, 
much faster than in the balancing portion, so I declared success and mounted 
it to the newly sealed pole-top unit.

WOW!  Nothing but whoosh, and in winds sufficient to make 25 Amps, not the 
first movement of tail flutter from dead calm up through whatever wind level 
that was (we don't have an anemometer at the unit - but the mast reading was 
in the mid to high 20s).  Ours is mounted on our arch, and in the past, we'd 
get vibration which would set the danforth we had on one of the pulpit rails 
singing against the rail, and our deck moaning, serenading us in our aft 
cabin below.  No such experience now.  As there was no change, effectively, 
from before to now (the receivers on the bearings should not have had any 
effect of this sort) in our re-do, I can only assume it was the balancing 
which did the trick.

I have another set of lead strips, so if, for whatever reason, our balance 
changes (weathering, some oddball chip, whatever), I can do it again. While 
we were VERY happy with our KISS before, we're ecstatic, now.  Those of you 
who happen to be in our cruising area this winter (southern Bahamas), when 
the northers are common, will have a chance to see it, and compare it to the 
many other KISS mounted on other boats.

John (Hotwire), before I broke down and bought the second spindle, suggested 
the factory balancing would be fine until I found another cruiser with one 
to loan me.  Based on my experience, I disagree.  I suspect vibration was 
what caused my bearing receiver in the nose to come out of its seat - and 
that was with a very satisfactory level of noise and flutter.  Norm's 
experience with vibration causing electrical problems might well have been 
avoided if the prop didn't have any vibration.

Oh, ya, one other fillip - seen from the side, the prop tips line up exactly 
when they're spinning.  John (Hotwire) tells me that's NEVER seen.  Mind 
you, I couldn't very well take a micrometer up there, but certainly, with 
the best an eyeball from 5' can tell, they are perfectly aligned.  I think 
it has to be the balancing.  YMMV :{))

L8R, y'all

Skip, over killer wifi in Marsh Harbour

Morgan 461 #2
SV Flying Pig KI4MPC
See our galleries at www.justpickone.org/skip/gallery !
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(and)
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(Richard Bach) 

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