Turns out it was a bad zener diode, Cut it out, and bam.... 11 psi green 
bars on the A/F and 1400 - 1500 degrees on the EGT gauge. We added in a 
front mounted intercooler, and now were running at about 13 psi, with the 
same egt's, stock inj's and MP logic module. So now were ready for the + 
40's and a calibration.

Sean B


----- Original Message ----- 
From: "Mike D." <[email protected]>
To: <[email protected]>
Sent: Sunday, September 20, 2009 10:45 AM
Subject: Re: SD> Fw: Lean Issues


>
> I guess I should do lots more research.  I haven't touched the car in a 
> very long time and haven't payed attention to tweaking trends in a very 
> long time either.
>
> I have an A/F gauge.  I suppose I should look into a custom cal using 
> larger injectors and a higher volume fuel pump with an adjustable FPR.
>
> What if I only use the 3" swing valve and downpipe with my current logic 
> module and the rest of the exhaust remaining stock/restrictive (for now)? 
> Think it will be ok for a little while?
>
> Side note:  the car is in many pieces, block on a stand, trani on a 
> pallet, hasn't been driven in years....so no immediate worry of melting 
> the thing ;)
>
> Thanks for the help.
>
>> From: [email protected]
>> Date: Sun, 20 Sep 2009 10:09:42 -0400
>> To: [email protected]
>> Subject: SD> Fw: Lean Issues
>>
>>
>> I would at least throw some +20s on there. You'll be moving a lot more 
>> air
>> with that big swingvalve and exhaust. I never tried the stock injectors 
>> but
>> with +20s I could only get my air-fuel ratio to about 12.5:1 which is a 
>> bit
>> lean. I was also running a manual boost controler at about 18 psi.
>>
>> That was my experience anyway. There are a lot more knowledgable people 
>> out
>> there than me though.
>>
>> I switched to DSM injectors and now I have plenty of fuel. I wouldn't try
>> stock injectors with the 3 inch SV and exhaust. Those pistons crack real
>> easy.  Do you have anything to monitor your air fuel ratio and boost 
>> with?
>>
>>
>>
>> In a message dated 9/20/2009 8:05:54 AM Eastern Daylight Time,
>> [email protected] writes:
>>
>> Message: 1
>> Date: Sat, 19 Sep 2009 23:04:48 -0400
>> From: "Mike D." <[email protected]>
>> Subject: Re: SD> Fw: Lean Issues
>> To: <[email protected]>
>> Message-ID: <[email protected]>
>> Content-Type: text/plain; charset="iso-8859-1"
>>
>>
>> Sorry for hi-jacking but, I'm working on putting my '87 CSX back together
>> and I was planning to use a 3" swingvalve and exhaust with a stock turbo 
>> and
>> injectors.  I have the csx mopar performance logic module (stage 1 ???).
>> This will cause a lean condition????  Please explain.  Sorry for being 
>> dumb.
>>
>>
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