My trusty computer on my Bridgeport started going flaky, so I put in the development computer I had used for PCIe and 64-bit testing. The automatic update of the .ini and .hal files crashed and left a big mess, so i had to do the joint conversion by hand.

That all seemed to go well, but now I've seen two problems.

When homing right after startup, I get intermittent "home switch inactive before start of latch move
j=0"

That could be some kind of timing issue, likely the old version didn't have this test.

And, the second one is that before homing, my jog pendant works fine. AFTER homing all axes,
it does not cause movement.  I looked at :
joint.0.jog-enable it goes true when the jog enable button is pressed joint.0.jog-scale it is 2.5x10^-5 (-r ^-6 or ^-7) depending on the jog rate selector joint.0.jog-counts it shows a large integer which changes as the jog dial is rotated.

Any idea why homing the axes makes LinuxCNC no longer accept changes to jog-counts?

Thanks,

Jon


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