My trusty computer on my Bridgeport started going flaky, so
I put in the development computer I had used for PCIe and
64-bit testing. The automatic update of the .ini and .hal
files crashed
and left a big mess, so i had to do the joint conversion by
hand.
That all seemed to go well, but now I've seen two problems.
When homing right after startup, I get intermittent "home
switch inactive before start of latch move
j=0"
That could be some kind of timing issue, likely the old
version didn't have this test.
And, the second one is that before homing, my jog pendant
works fine. AFTER homing all axes,
it does not cause movement. I looked at :
joint.0.jog-enable it goes true when the jog enable button
is pressed
joint.0.jog-scale it is 2.5x10^-5 (-r ^-6 or ^-7) depending
on the jog rate selector
joint.0.jog-counts it shows a large integer which changes
as the jog dial is rotated.
Any idea why homing the axes makes LinuxCNC no longer accept
changes to jog-counts?
Thanks,
Jon
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