Hi Dave,
 
I don't quite follow your reasoning, looking at the traces Thomas posted 
above I can see that the second trace down (U15_SELSECOND) drops to a low 
state
followed by a falling edge of U15 WR* on the third trace down, at this 
point the NOR gate U15A effectively turns the falling edge into a rising 
edge to trigger the flip flop, satisfying the condition you mentioned.
 
What Thomas has achieved is to introduce about 20nS (10nS per gate for 
74LS) of propogation delay into the flip flop clock signal which seems to 
be just enough for the data lines to settle.
 
Triggering on a wisker, you bet !!
 
I still don't think this is an IDE card issue, but it can be patched to 
accomodate the problem
 
best regards
 
David Fry

On Monday, June 9, 2014 8:58:03 PM UTC+1, yoda wrote:

> I think the problem stems from the S100 signals are valid on falling edges 
> and the FF is valid on rising edge.  I am not sure the fix is general 
> purpose yet.   I think inverting the clock to the FF would be a general 
> purpose solution.  I don't see a spare inverter left on the board - but 
> probably can build one out of spare gates which I think Thomas may have 
> effectively done - I need to work through the signals to verify - of course 
> the Logic analyzer will answer the question quickly as well. 
>
> Dave
>
>
> On Monday, June 9, 2014 2:52:45 PM UTC-5, David Fry wrote: 
>>
>>  Hi Thomas,
>>  
>> nice fix :-)
>>  
>> I'm no S-100 bus signalling expert but I would have logically expected 
>> the Data lines to be settled and valid at the point in time the WR* signal 
>> goes low, this would seem to not be the case in this instance. I don't see 
>> this as a fault in the IDE card design but rather that the device driving 
>> the card (CPU card) is not performing as we would expect.
>>  
>> Part of the fun of mixing old and new technology perhaps ???
>>  
>> regards
>>  
>> David Fry
>> On Monday, June 9, 2014 8:27:54 PM UTC+1, Thomas Owen wrote:
>>
>>> UPDATE:
>>>
>>> As  mentioned, I set up a delay by using the 2 unused gates on the 
>>> 74LS02 to delay the clock signal to the flip flop.  *Drive selection 
>>> now works perfectly*.
>>>
>>> I will see if I can get a screen shot from the analyzer showing the 
>>> relationship of DO0 to the clock, but for now, here is what I did:
>>>
>>> U15 pin 1 -> U15 pin 5/6  | U15 pin 4 -> U15 pin 8/9 | U15 pin 10 -> U16 
>>> pin 3
>>>
>>> Thomas
>>>
>>>
>>> On Sunday, June 8, 2014 7:58:45 PM UTC-4, Thomas Owen wrote: 
>>>>
>>>> All,
>>>> I had posted this to the thread dealing with ordering this card, but 
>>>> decided to post a new topic dealing with the problem I have had with final 
>>>> checkout of the board. 
>>>>
>>>> During assembly the board passed all the 'in progress' checks.  The 
>>>> final steps were to output to different ports:
>>>>
>>>>
>>>> I have output the following and everything passes:
>>>>
>>>> QO33,80 ; Configures ports A, B and C as output ports
>>>> QO32,2B ; Selects right hand pair of digits
>>>> QO30,01; display 01on right digit pair and work through each bit - all 
>>>> ok
>>>>
>>>> QO32,2c; Selects middle pair of digits
>>>> QO30,01; Should display 01 on middle digit pair, work through each bit 
>>>> - all ok
>>>>
>>>> QO32,2d; Selects left hand pair of digits
>>>> QO31,01; Should display 01 on left digit pair, work through each bit - 
>>>> all ok
>>>>
>>>> All displays are correct.
>>>>
>>>> Now the final step is the Drive Select and that is where I am having 
>>>> trouble:
>>>>
>>>> Board always comes up with 'Drive A' selected
>>>>
>>>> Now,  QO34,0; no change
>>>>
>>>> Reset, start again:
>>>>
>>>> QO34,1; no change
>>>>
>>>> I can never select drive B.   
>>>>
>>>> Several generous members (thank you David Fry) have made suggestions, 
>>>> and here is where I now stand:
>>>>
>>>> My preliminary check this afternoon shows me that there is a timing 
>>>> issue at U15, the 74ls02.  Using my logic analyzer and monitoring the 
>>>> inputs and the output (which clocks the drive select flip flop) I see a 
>>>> big 
>>>> timing difference between SEL_SECOND and WR.
>>>>
>>>> What this means is that the output of the gate never goes high allowing 
>>>> the bit change to effect drive change/selection.
>>>>
>>>> I am going to get some screen shots from the analyzer tomorrow, and if 
>>>> anyone has any suggestions I would greatly appreciate it.
>>>>
>>>> Thanks,
>>>> Thomas
>>>>
>>>>        

-- 
You received this message because you are subscribed to the Google Groups 
"N8VEM-S100" group.
To unsubscribe from this group and stop receiving emails from it, send an email 
to [email protected].
For more options, visit https://groups.google.com/d/optout.

Reply via email to