Here is my hal file. I am currently getting the error "3D.post.gui.hal:4 
Pin 'pyvcp.E0.Temp.set' does not exist." And I am not totally sure what 
that all means, Sorry!
I took the standard CRAMPS CNC configuration files, and used the deracking 
MPCNC settings to try and setup deracking on the Y-gantry.


On Thursday, March 28, 2019 at 10:46:38 AM UTC-4, Paulo Sherring wrote:
>
> Hey there! I guess it would help if you post your hal file, set debug to 5 
> and post your debug output.
> Best regards.
>
> Em quinta-feira, 28 de março de 2019 10:34:18 UTC-3, Bradley Turner 
> escreveu:
>>
>> Hello,
>> I am trying to setup a similar config on my machine, although I only have 
>> a gantry config on the X axis. Every time I change something in the .hal 
>> file I will no longer be able to get machinekit to boot. It will show the 
>> splashscreen and then never load the AXIS gui. I am very new to Linux CNC, 
>> so any help would be greatly appreciated.
>>
>> On Monday, October 16, 2017 at 9:55:21 PM UTC-4, Tom M wrote:
>>>
>>>
>>> I finally got my homing and deracking tuned for my dual gantry MPCNC.
>>> Here's a video:
>>> https://youtu.be/FRT0teFvGy8
>>>
>>> (Thanks Charles, for your wonderful work)
>>>
>>>
>>>
>>> On Saturday, September 30, 2017 at 7:16:20 PM UTC-5, Tom M wrote:
>>>>
>>>> Well the Milwaukee Makerfaire is done, I had my MPCNC running for 2 
>>>> days straight and I was fair pleased with how it ran.
>>>> At the time I only had auto-homing working on the x but that's all 
>>>> fixed now.
>>>>
>>>> If someone wants use an  MPCNC with Machinekit and a Cramps  on a 
>>>> beaglebone you can find it here: 
>>>> https://github.com/Workshop88/MPCNC/tree/AutoHoming
>>>> Its not perfect and I'm not done, but it works.   One issue I had was 
>>>> that the motors would skip after a the carriage deracked and it was 
>>>> returning to the home position.  I could keep if from skipping by keeping 
>>>> the home distance short.  It seems that this mode doesn't respond to max 
>>>> job speed or max velocity overide in axis display.   I'm assuming the fix 
>>>> is just to reduce the max velocity settings.
>>>>
>>>>
>>>>
>>>> On Tuesday, September 19, 2017 at 11:53:28 PM UTC-5, Tom M wrote:
>>>>>
>>>>> Well, I'm doing my happy dance..
>>>>> My current issue is I didn't have my xenable signal tied into my 
>>>>> enable, powerup and led on my cramps board... (Thanks for the hints but 
>>>>> not 
>>>>> the answer) Now I'm getting dangerous since I'm starting to think I 
>>>>> almost 
>>>>> know what I'm doing...  
>>>>> I'm able to jog and do manual homing...Next step I need to get my 
>>>>> switches wired up and working on the autohoming.  I'm hoping I can get 
>>>>> this 
>>>>> ready for the Milwaukee makerfaire without pulling an all nighter or 
>>>>> two....  Hoo hoo
>>>>
>>>>

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Attachment: CRAMPS.hal
Description: Binary data

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