It sounds like not everything is getting mapped on start up. Are you building an MPCNC or something with just single axis deracking. Are you using a cramps board?
On Thu, Mar 28, 2019, 10:19 AM Bradley Turner <[email protected]> wrote: > Here is my hal file. I am currently getting the error "3D.post.gui.hal:4 > Pin 'pyvcp.E0.Temp.set' does not exist." And I am not totally sure what > that all means, Sorry! > I took the standard CRAMPS CNC configuration files, and used the deracking > MPCNC settings to try and setup deracking on the Y-gantry. > > > On Thursday, March 28, 2019 at 10:46:38 AM UTC-4, Paulo Sherring wrote: >> >> Hey there! I guess it would help if you post your hal file, set debug to >> 5 and post your debug output. >> Best regards. >> >> Em quinta-feira, 28 de março de 2019 10:34:18 UTC-3, Bradley Turner >> escreveu: >>> >>> Hello, >>> I am trying to setup a similar config on my machine, although I only >>> have a gantry config on the X axis. Every time I change something in the >>> .hal file I will no longer be able to get machinekit to boot. It will show >>> the splashscreen and then never load the AXIS gui. I am very new to Linux >>> CNC, so any help would be greatly appreciated. >>> >>> On Monday, October 16, 2017 at 9:55:21 PM UTC-4, Tom M wrote: >>>> >>>> >>>> I finally got my homing and deracking tuned for my dual gantry MPCNC. >>>> Here's a video: >>>> https://youtu.be/FRT0teFvGy8 >>>> >>>> (Thanks Charles, for your wonderful work) >>>> >>>> >>>> >>>> On Saturday, September 30, 2017 at 7:16:20 PM UTC-5, Tom M wrote: >>>>> >>>>> Well the Milwaukee Makerfaire is done, I had my MPCNC running for 2 >>>>> days straight and I was fair pleased with how it ran. >>>>> At the time I only had auto-homing working on the x but that's all >>>>> fixed now. >>>>> >>>>> If someone wants use an MPCNC with Machinekit and a Cramps on a >>>>> beaglebone you can find it here: >>>>> https://github.com/Workshop88/MPCNC/tree/AutoHoming >>>>> Its not perfect and I'm not done, but it works. One issue I had was >>>>> that the motors would skip after a the carriage deracked and it was >>>>> returning to the home position. I could keep if from skipping by keeping >>>>> the home distance short. It seems that this mode doesn't respond to max >>>>> job speed or max velocity overide in axis display. I'm assuming the fix >>>>> is just to reduce the max velocity settings. >>>>> >>>>> >>>>> >>>>> On Tuesday, September 19, 2017 at 11:53:28 PM UTC-5, Tom M wrote: >>>>>> >>>>>> Well, I'm doing my happy dance.. >>>>>> My current issue is I didn't have my xenable signal tied into my >>>>>> enable, powerup and led on my cramps board... (Thanks for the hints but >>>>>> not >>>>>> the answer) Now I'm getting dangerous since I'm starting to think I >>>>>> almost >>>>>> know what I'm doing... >>>>>> I'm able to jog and do manual homing...Next step I need to get my >>>>>> switches wired up and working on the autohoming. I'm hoping I can get >>>>>> this >>>>>> ready for the Milwaukee makerfaire without pulling an all nighter or >>>>>> two.... Hoo hoo >>>>> >>>>> -- > website: http://www.machinekit.io blog: http://blog.machinekit.io github: > https://github.com/machinekit > --- > You received this message because you are subscribed to a topic in the > Google Groups "Machinekit" group. > To unsubscribe from this topic, visit > https://groups.google.com/d/topic/machinekit/To6ivNZpEHU/unsubscribe. > To unsubscribe from this group and all its topics, send an email to > [email protected]. > Visit this group at https://groups.google.com/group/machinekit. > For more options, visit https://groups.google.com/d/optout. > -- website: http://www.machinekit.io blog: http://blog.machinekit.io github: https://github.com/machinekit --- You received this message because you are subscribed to the Google Groups "Machinekit" group. To unsubscribe from this group and stop receiving emails from it, send an email to [email protected]. Visit this group at https://groups.google.com/group/machinekit. For more options, visit https://groups.google.com/d/optout.
